Changes to book pages and site clean up

 

edleft.jpg (2193 bytes)I’ve changed the book reviews and listings for  gun related firearms and I am starting to include other sources besides Barnes &  Noble. I started to run into too many instances where books were listed as “requires  special handling”, or “book out of print – special order” when I knew, for  a fact, books were readily available, at lower prices, from numerous other legitimate  sources.

I went through and sorted out the site,  including most of the archive pages. I had noticed some detached links and missing images  that were caused by my moving things around on the site. If you run into similar problems  in the future, please just let me know and I’l get the problem squared away.

Ruger Bisley – Trigger  Improvements II

I just wanted to note as a reminder – The  basis for this short series of articles was to see if an amateur firearms enthusiast could  reasonably complete a trigger job on a Ruger single action revolver. The text is a  reflection of my understanding of the task, and is to be considered an experiment until  completed and the gun checks out for proper safety and operation. The last installment  will be a summary of the process and correction to and information or early conclusions  that might have been in error.

Two steps forward, one step back. I had a  Ruger manual, a disassembly guide, a copy of “Gunsmithing: Pistols and  Revolvers”, and the documentation that came with the Wilson hammer/trigger rework  fixtures – none of this provided enough information for me to begin work on any of the  parts. I don’t know if single action revolvers are as sensitive to alterations as 1911  design pistols, but trigger work can impact a gun’s safe operation, and quality of  function.

For a gun design that’s been around for a  very long time, it’s difficult to locate anything published on Ruger’s single action  revolvers that would offer enough detail to be useful in making modifications. A person  working on any modern auto pistol or double action revolver could select from an almost  endless list of publishers and authors. In fact, if I wanted to work on any Ruger double  action, auto, .22 pistol or rifle I could select from books, charts and video for  guidance.

I was disappointed with the documentation that came with the Wilson fixtures from  Brownells. I suppose the argument could be made that these tools are typically used by  experienced gunsmiths, but I think that’s not a valid excuse for the manufacturer.

Machinists, and any other person involved in  the modification of parts, requires accurate drawings, illustrations and explanations,  before jumping in and hacking up parts. Whoever purchases the fixture is entitled to a  quality representation of how it should be set up, and to what specs parts should be  reworked.


The picture on the right is the actual part and fixture, supposedly represented  by the sketch. Er..if that drawing illustrates how to properly modify that little notch  (1) I must be missing something. The text goes on to advise of steps such as, “whet  with 400 – 500 stokes.” I just don’t know how the number of stokes would get anyone  to a specific finish, dimension, parallel surface, etc.

It would be nice if the folks who sell these  products spent a couple of hours writing some decent representation of its intended use,  better still, maybe include a couple of “before and after” pictures of  parts and proper setup, maybe even highlighting critical areas.

I assembled and disassembled the Ruger  several times. I put parts in the fixtures and worked the action without springs in place.  I took a look through several reference books that illustrated theory of operation for the  single action revolver until finally it all sank in, and I was comfortable enough with the  operation of the gun to understand the purpose of the modifications and the projected  results.

I  started the rework setup with the #16 jig for the hammer. The fixture has two parts; a  machined block and a steel pin. The pin passes through the hammer pivot opening, and is  used to align and properly position the hammer in the block. The pin was a tight fit, not  a press fit, but a snug fit, which seems right for keeping parts aligned.

There is a groove in the top of the fixture the pivot pin rests in during the  rework. There are set screws that pass through the bottom surface of the block and project  into the groove. The distance from the projecting screws to the upper surface of the block  should be .101″, to properly locate the pin and hammer. These dimensions should be  verified before the fixture is used. Checking with a depth mic, one was right on at  .101″, the other was .005″ low.

Combining the two fixture parts with the hammer should result in something that  looks a lot like this. Unfortunately the hammer, when mounted to the pin, wouldn’t rotate  through full travel without making contact with the block. This contact forced the pin  away from the block on the left side (1), moving the hammer out of proper position.

It looked as though the hammer plunger was  bumping against the set screw in the center vertical groove in the block, forcing the  hammer out of position. I removed the hammer plunger.

Removing the plunger assembly is a pretty easy deal. You hold the hammer in one  hand, hold a small punch to the plunger retention pin with the other hand, then use your  other free hand to tap the pin out. Yes, I know.

The plunger is spring loaded, so you want to  be careful it doesn’t pop out and fly across the room. On the other hand, the plunger  spring may not fall out when the plunger is removed, but it will drop out while your  working on the hammer, and immediately roll under an immovable object.

With the plunger removed, I dropped the  hammer back in the fixture, but it was still binding against some surface of the block. A  little further investigation, and I could see the contact was with the lower right front  edge of the block’s vertical slot.

You can see how crooked the fixture slot was cut with (1) shifted toward the left  and creating the interference. I do not believe this shift was to accommodate an offset in  the hammer, and a .015″ machining error was enough to prevent proper use of the  fixture.

Most fitting and filing fixtures are made  for production, and are surface hardened to prevent them from prematurely wearing in  normal use. I thought I might just exchange the fixture for one that wasn’t defective  because I thought the hardened surface would make metal removal difficult. It took exactly  4 stokes with a fine file to clear the .015″ problem, and arrive at the conclusion –  the fixture was not surface hardened. 

wpe55.jpg (7648 bytes)If this were a 1911 type auto, we’d be looking  for sear/hammer engagement. The single action Ruger incorporates the sear function into  the trigger.

The #17 fixture, a sear block, permits trial  fitting of parts and checking for engagement between hammer and trigger, without having to  constantly reassemble the pieces into the gun.

The rework objective is to get .012″ –  .014″ engagement at (1) and (2), and to reduce friction.

The fixture instructions suggested adjusting the hammer’s full cock notch  .030″ “or more” above the fixture’s surface, placing a square India stone  against the hammer, and measuring the gap with a feeler gauge.

I tried the stone and feeler gauge method, and I verified with a dial indicator.  There was .022″ engagement with my hammer, trigger combination and,   and the  full cock notch contact areas were rough and uneven.

In the front view photo, you can see how uneven the part was ground and how rough  the metal was at the groove, or point of contact. This condition would create high trigger  pressure, creep and a rough feel. In the first installment of the article, I noted I had  purchased a fine and extra fine square stone. After I got the fixtures and walked through  the rework, I realized I needed a triangle shaped stone to clean up the full cock notch.

I ordered a Norton India stone from Brownells.  Unlike the first two ceramic stones that use water for lubrication, the new stone uses  honing oil.

 

With the hammer mounted securely in the fixture, the full cock notch is adjusted  down to between .012″ – .014″. This is done by stoning the area of the hammer  immediately below the notch, measuring frequently as the work progresses. It is important  for the stone to be kept parallel to the surface to insure the .012″ – .014″  dimension is held all the way across the notch, insuring a complete contact surface with  the trigger sear.

I found the area immediately under the full cock notch was relatively easy to  hold parallel while stoning, but it was difficult to blend the resulting flat into the the  area further down from the notch.

I put a sheet of glass on the bench, placed  the hammer on the glass with the thumb grip area hanging off the edge, so the hammer was  resting on it’s flat side surface. Then I drew the stone over the surface I wanted to  blend and keep parallel. Worked out really nice and I used the same technique on some of  the other clean up.

Cleaning up the actual full cock notch was a concern because the Wilson fixture  set the hammer at an odd angle to the surface that would guide the triangular stone. I was  concerned the angle of contact would be off and reduce the surface area supporting the  cocked hammer.

The notch is tipped down, toward the fixture  surface and, while the stone is held parallel to the fixture surface. I kept the notch  approximately .002″ above the fixture surface, used a large magnifying lens, and  exercised a great deal of care with the stone. It only took a couple of touches to remove  the manufacturing tool marks and clean up the notch.

This is the finished hammer, or at least as finished as I could get with my  limited skill and experience. The area in the yellow circle was stoned to reduce the the  full cock notch to .014 “, the notch was cleaned of tool marks and made parallel to  the trigger sear. The angle of the notch was not changed in any way.

The surface immediately above the notch has  been smoothed, but this is not really critical since it is not a contact surface, but the  trigger sear drags across this surface under load, so surface should be uniform

Reducing the contact area of the full cock  notch and smoothing that surface are important steps. The quality of finish will have a  direct impact on trigger pull. Under spring load, with low mechanical advantage, a small  burr, or an area worn rough, can feel like you’re pulling a trigger over gravel

On the left is a close up of  the trigger and hammer set placed on the sear  block so engagement could be checked. Throughout the rework process, a candle was used to  blacken contact surfaces, then the parts were cycled and rub marks were inspected as an  indication of proper engagement.

If you look closely, you can see a vertical  mark running down the face of the trigger sear. This is an indication of full contact and  parallel surfaces.

This particular check was done after the  hammer work was completed, but prior to any work being done on the trigger.

Next, the Wilson #15 fixture was used to  accomplish the rework on the trigger. As received, the trigger would not locate correctly  in the fixture. When the sear position was set correctly, the tab on the side of the  trigger contacted  the rear surface of the fixture, preventing the fixtures locating  pin from being installed.

#15 is a simple rectangular block, slotted,  cross drilled and fitted with a set screw. The trigger slides into place with the sear  pointing straight up. The set screw is adjusted to place the sear surface parallel to the  surface of the fixture. As illustrated to the far right, the clearance slot was inadequate  and did not allow the trigger to be properly aligned. I removed a small amount of material  from the recess, maybe .020″ and the trigger fit in place correctly.

On the left is the finished trigger. When completed, it mated correctly with the  hammer full cock notch, fully across the face, and both part surfaces were parallel to one  another. The trigger was a little difficult. There were many deep tool marks and the  fixture did little to help create a parallel face. I found it best to run 50 or 60 stokes  with the stone, then turn the fixture around, and make the next 50 or 60 strokes from the  other direction. The final cut was to put a 45 degree bevel across the sear, opposite the  engagement edge.

I’m going to break at this point, with all  of the parts completed, and only reassemble and live testing remaining. Should have it all  wrapped up next time around. Hopefully, the results of the trigger job will be quantified  and I may even have some suggestions for a better set of jigs and fixtures.

 

 

Thanks,
Joe

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